^ very funny,
wow, what terrible conditions, but you guys already knew that, inspite of it all It was great fun seeing everyone and running at the new track.
unfortunately the track is terrible with sudden elevation changes(bumps), and thats nothing to do with the conditions, the wind was relentless and never let down,
I had lots of troube from the start of the whole weekend, I guess when my car took four hrs to idle right I should have seen the signs, clearly she didnt want to go to beeville
however she made a lot of power I will post up the dyno number and graph later, but at the end of the night on friday after multiple pulls on the hot humid weather in houston, she made 1121 hp to the wheels with nearly 1000 ft lbs of torque all around 4000 rpm! it was unfortunate that I could not harness that power and put it to good use(kick mullets butt
) but as tomy said the saga continues
the tune may be off a little as when we pulled the plugs the car seemed to be running lean and one of the spark plugs was completly melted off, however no apparant engine damage, I borrowed a plug from chip and she fired right up idled fine and jumped right back on the trailer to come home, she is put away now and Im really tired I think I got 7 hrs of sleep in the last three days!
thanks again to everyone that helped out chip, tomy, mark H, and yes mullet too I guess
I cant say I will be back to the next texas mile if the condition remain the same and im not talking about the wind, but rather the track.
one last note I like to mention, if it wasnt for bill at DA I would have not been able to make the trip, he was on the phone with me all night before we left guiding me through the challenging sc belt swap, I like to thank him as well.