The block off plates were probably an attempt to prevent suction of hot air from the engine compartment into the the engines intake. Not a good idea, as others have posted it can cause turbulent air to upset the MAF readings. Engineers at major car companies don't add costs to the cars without good reason. The part was designed that way for a good reason.
... I feel pretty sure that a Hefner turbo setup will solve the problem.
Questions...answers:
I did not notice any engine light.
I used the SCT Tuner device and the car did not report any error codes.
The car has been "ruining" well. It recently dyno'd at 621hp and event the day it died 3 times it ran well on the road
The gas tank was at least 3/4 full
When I was in the garage tonight looking the car over for clues I notice that the coolant has a strange substance in it (I added water wetter but I don't think that is what I am seeing). It looked a bit like oil :ack
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I dont know a lot about mechanics but Im guessing that problem only happens when Im not moving because I am not on the accelerator when Im not moving. Wouldnt having the throttle depressed prevent that problem from occurring?
The dealer did inspect/test the new fuel filler for cracks this past time and didnt find any.
Is the tune also a possibility? My next two steps are to remove the block off and get a custom dyno tune instead of the generic tune that several tuners use.
Im not too familiar with working on the car so Im going to need pretty specific directions to check the ground wire issue. Might have the guys check it when i take it in for a dyno tune next week.
Either way, a lot of you have been way more helpful with the diagnosis than the dealer was. I really appreciate it. Hopefully, I have this problem nailed down by next week.
Kumar received the P1000 code not me.
My battery cable was tight as a whip and the car has stock filters. Given that this has only occurred within the last week, I think I will run a full tank of gas though it before I get really concerned.
Well there is chance I might have solved my problem. Ground wire was already tight. Took out the blockage from the air vent and went for a drive.
On a 30 minute city drive, the car didnt die once. It did dip down to 400rpm once but Im guessing a little play in the idle is normal.
edit: I still plan to check the filter and get a tuner to play with the idle parameters. Too bad its going to be freezing the next few days.
The fuel neck on the car has already been replaced. Also, this past week the dealer checked the new fuel neck again for any possible cracks and also did a smoke test. Id be shocked at the dealer's incompetence if that is still the problem.