I have been anxious to test the Granatelli Motor Sports 4V coil pack system since Tony @ HP Performance first told me about them a month or so ago.
On paper and on their website video they looked real good. Unfortunately for me, the results were mediocre. I have displayed 8 runs on this graph to give you an idea.
RUNFIL~3.DRF: Stock coils. TR7-IX plugs @ .030". The Max Power on this run should be 771.70 and not 782.07. The 782.07 was a spike at the end of the run and not valid.
RUNFIL~5.DRF: GMS coils. TR7-IX plugs @ .030". First run with GMS coils. Lost a little power.
RUNFIL~6.DRF: GMS coils. TR7-IX plugs @ .035". According to the instructions, they recommended experimenting with increasing the plug gap by .005" to .010". It didn't sound good above 6200 rpm.
RUNFIL~7.DRF: GMS coils. TR7-IX plugs @ .030". Besides closing down the plug gap, I leaned out the A/F a little and the results were good. This time it sounded good above 6200 rpm.
RUNFIL~8.DRF: GMS coils. TR7-IX plugs @ .030". A duplicate of the prior run.
RUNFIL~9.DRF: GMS coils. TR6 plugs @ .028". Just for kicks and grins, I put in the plugs from my previous dyno session. Basically no change.
RUNFI~12.DRF: Next day. Stock coils. TR7-IX plugs @ .030". I wanted to check the stock coils again. There was a small increase in power over the last run from the previous day.
The conditions were a little bit different on this day as compared to the previous day. On the previous day, the ABP=29.8 / Temp=55.2* / Humidity=51%. On this day, the ABP=29.5 / Temp=52.8* / Humidity=49%. On the previous day the SAE correction factor was 96.2% and on this day it was 97%.
When I was removing the GMS coils from the car, the ear on one of the coils cracked and broke loose. The attachment of the coil to the "rope" and the "rope" to the spark plug is much more positive with this system and requires some effort to detach the coil assembly from the spark plug. Now I see why the stock ones are so easy to remove.
The bottom line is very little to no difference when running the GMS coil packs. Like I said, disappointing. A lot of work for no payback. Oh well, this it was testing is all about. At least I didn't lose any significant power like the next run.
RUN_FI~13.DRF: Stock coils. TR7-IX plugs @ .030". K&N filters. This run was actually worse than it looks. As soon as I put on the filters, the car ran like crap. It was hunting up and down at an idle and almost died. It was struggling to maintain an A/F of 14.7 in closed loop. When shifting gears, the motor wanted to die when I let off. The A/F during the run was very rich. These filters are very restrictive when compared to the stock ones. Looking at them, you can see that they have less sq.inches of filtering material. Once again, the results speak for themselves. I made one more run with the factory filters and the numbers were back up where they belong and the idle was smooth and clean.
Well, there you have it. In terms of finding more power, this was a waste of two days. That is all the dyno testing for me for now. I am quite satisfied with the overall results of the Whipple install and I can't stand having to wait before I am able to drive the car. When the weather finally does clear up (springtime) I will be heading out to the drag strip to see how many runs I can get in before they kick me out.:biggrin
Steve
On paper and on their website video they looked real good. Unfortunately for me, the results were mediocre. I have displayed 8 runs on this graph to give you an idea.

RUNFIL~3.DRF: Stock coils. TR7-IX plugs @ .030". The Max Power on this run should be 771.70 and not 782.07. The 782.07 was a spike at the end of the run and not valid.
RUNFIL~5.DRF: GMS coils. TR7-IX plugs @ .030". First run with GMS coils. Lost a little power.
RUNFIL~6.DRF: GMS coils. TR7-IX plugs @ .035". According to the instructions, they recommended experimenting with increasing the plug gap by .005" to .010". It didn't sound good above 6200 rpm.
RUNFIL~7.DRF: GMS coils. TR7-IX plugs @ .030". Besides closing down the plug gap, I leaned out the A/F a little and the results were good. This time it sounded good above 6200 rpm.
RUNFIL~8.DRF: GMS coils. TR7-IX plugs @ .030". A duplicate of the prior run.
RUNFIL~9.DRF: GMS coils. TR6 plugs @ .028". Just for kicks and grins, I put in the plugs from my previous dyno session. Basically no change.
RUNFI~12.DRF: Next day. Stock coils. TR7-IX plugs @ .030". I wanted to check the stock coils again. There was a small increase in power over the last run from the previous day.
The conditions were a little bit different on this day as compared to the previous day. On the previous day, the ABP=29.8 / Temp=55.2* / Humidity=51%. On this day, the ABP=29.5 / Temp=52.8* / Humidity=49%. On the previous day the SAE correction factor was 96.2% and on this day it was 97%.
When I was removing the GMS coils from the car, the ear on one of the coils cracked and broke loose. The attachment of the coil to the "rope" and the "rope" to the spark plug is much more positive with this system and requires some effort to detach the coil assembly from the spark plug. Now I see why the stock ones are so easy to remove.
The bottom line is very little to no difference when running the GMS coil packs. Like I said, disappointing. A lot of work for no payback. Oh well, this it was testing is all about. At least I didn't lose any significant power like the next run.
RUN_FI~13.DRF: Stock coils. TR7-IX plugs @ .030". K&N filters. This run was actually worse than it looks. As soon as I put on the filters, the car ran like crap. It was hunting up and down at an idle and almost died. It was struggling to maintain an A/F of 14.7 in closed loop. When shifting gears, the motor wanted to die when I let off. The A/F during the run was very rich. These filters are very restrictive when compared to the stock ones. Looking at them, you can see that they have less sq.inches of filtering material. Once again, the results speak for themselves. I made one more run with the factory filters and the numbers were back up where they belong and the idle was smooth and clean.
Well, there you have it. In terms of finding more power, this was a waste of two days. That is all the dyno testing for me for now. I am quite satisfied with the overall results of the Whipple install and I can't stand having to wait before I am able to drive the car. When the weather finally does clear up (springtime) I will be heading out to the drag strip to see how many runs I can get in before they kick me out.:biggrin
Steve